1. 北京航空航天大学机械工程及自动化学院,北京,100191
2. 北京航空航天大学江西研究院,南昌,330096
3. 南昌航空大学,南昌,330063
4. 南昌沪航工业有限公司,南昌,330063
纸质出版:2025
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马文硕,张瑾丰,张志超,杨毅青,邢普,危震坤. 面向角铣头抑振的两自由度动力吸振器设计与试验[J]. 航空制造技术, 2025, 68(12): 68-74,81.
MA Wenshuo, ZHANG Jinfeng, ZHANG Zhichao, YANG Yiqing, XING Pu, WEI Zhenkun. Design and Experiment of Two-Degree-of-Freedom Tuned Mass Damper for Chatter Suppression of Angle Milling Head[J]. Aeronautical Manufacturing Technology, 2025, 68(12): 68-74,81.
马文硕,张瑾丰,张志超,杨毅青,邢普,危震坤. 面向角铣头抑振的两自由度动力吸振器设计与试验[J]. 航空制造技术, 2025, 68(12): 68-74,81. DOI: 10.16080/j.issn1671-833x.2025.12.068.
MA Wenshuo, ZHANG Jinfeng, ZHANG Zhichao, YANG Yiqing, XING Pu, WEI Zhenkun. Design and Experiment of Two-Degree-of-Freedom Tuned Mass Damper for Chatter Suppression of Angle Milling Head[J]. Aeronautical Manufacturing Technology, 2025, 68(12): 68-74,81. DOI: 10.16080/j.issn1671-833x.2025.12.068.
作为一种能够有效提升机床加工范围和适应性的特殊刀柄,角铣头被广泛应用于飞机复杂结构件的加工。然而,其大长径比造成的弱刚度极易在实际加工过程中引发切削颤振,严重影响加工效率和精度。为此,设计了一种外装于角铣头的两自由度动力吸振器,旨在以最小化结构改动实现角铣头两正交方向的振动与切削颤振的高效抑制。基于实测角铣头动力学特性,建立了角铣头– 吸振器动力学模型。在此基础上,通过开展数值优化对吸振器的最优动力学参数进行求解。针对角铣头振型特征,采用图谱法对动力吸振器进行构型设计,并对样机开展有限元仿真。最后分别开展模态试验与切削试验,对动力吸振器的有效性进行验证。试验结果表明,加装动力吸振器后,角铣头末端频响函数峰值降低了73.5%,稳定切深增加了300%(主轴转速为1000 r/min时,由加装前的0.4 mm增至加装后的1.6 mm)。
The angle milling head
a specialized tool capable of expanding machining range and improving adaptability of machine tools
is extensively applied in the machining of complex aircraft structural components. However
its high length/diameter ratio often leads to low rigidity
making it highly susceptible to chatter during actual machining processes
which severely impacts machining efficiency and accuracy. A two-degree-of-freedom (two-DOF) tuned mass damper (TMD)
externally mounted on the angle milling head with minimized structural modifications
is specifically designed for suppressing vibration of the angle milling head along two orthogonal axes and milling chatter. Based on experimental measurements of the angle milling head’s dynamics
a dynamic model for the angle milling head–TMD system is developed. Numerical optimization is then carried out to determine the optimal dynamic parameters for the TMD. A configuration design for the two-DOF TMD is performed using the graphical approach according to mode shapes of the angle milling head
followed by finite element simulations of the TMD prototype. Finally
modal tests and cutting experiments were conducted to validate effectiveness of the TMD. Experimental results demonstrate that after installation of the TMD
the maximum magnitude of the frequency response function measured at the end of the angle milling head decreased by 73.5%
while the stable cutting depth increased by 300% (from 0.4 mm to 1.6 mm at spindle speed of 1000 r/min).
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